|
#1
|
|||
|
|||
Quote:
Make sure the alarm set button is pushed all the way! |
#2
|
|||
|
|||
The schematic is available online (thanks Bill J.) for anyone that wants to take a look.
https://app.box.com/s/e22uy20wf2slx63b8hlm . |
#3
|
|||
|
|||
Quote:
The Chassis on my radio is 7J03 and the service manual you linked to me was for a 7Z03 which I'm not sure what all the differences are exactly but there must of been some other wise they wouldn't of revised the chassis design from the 7J03 to the 7Z03, but from the looks of it one of the differences was possibly the addition of an extra knob of some sort to the side of the radio cabinet, which mine doesn't have. Last edited by vortalexfan; 09-21-2018 at 07:12 PM. |
#4
|
|||
|
|||
Well I have a good head start in recapping this radio, I have all but 3 of the coupling capacitors replaced (2 of them I won't bother with becuse they're just going across the AC Input to ground, one on each side of the AC plug hookup on the chassis, and they don't look like they are in that bad of shape, so I won't bother replacing them for right now).
The power supply caps might be a little trickier to place in the radio because there isn't very many places for one to place the new filter caps under the chassis as far as grounding the negative leads of the filter caps to. Also the wires and resistors and capacitors that were connected to the original can capacitors leads don't have much in the way of leads on them to go by for connecting them to the new capacitors. And I replaced the old selenium rectifier with a 1N4007 rectifier diode under the chassis, but left the old Selenium rectifier in place for appearances sake, same for the old can capacitor. |
#5
|
|||
|
|||
OK so I finally finished recapping the radio and went to plug it in and something made a sizzling noise in the radio and it started smoking so I quickly turned it off and unplugged it and took it apart to see what happened and nothing looked burned inside the radio, all of the filter caps were fine (they none of them were reversed) the 1N4007 Diode still looked good and it wasn't reversed and like I said nothing else looked burnt inside the radio, component wise.
The clock and the neon pilot light still work but the tubes aren't glowing so I don't know if maybe a tube failed or what, but either way its kind of got me stumped because nothing inside the radio looks burnt and none of the stuff that I thought of that could of caused that issue was the cause. Any ideas as to what could of happened? See photo below for the finished recap job. Last edited by vortalexfan; 10-01-2018 at 06:46 PM. |
Audiokarma |
#6
|
|||
|
|||
Quote:
I have almost the same radio that I have to get back to. |
#7
|
|||
|
|||
Quote:
So it's kind of hard to test the radio chassis outside the case. |
#8
|
|||
|
|||
Quote:
The funny thing is that when I test the old capacitor's leads they test normal, no shorts or anything, charge up to over 15 Megaohms and then slowly discharge like they're supposed to. I might put it back together and see if it was maybe just a fluke. EDIT: just put it back together and tried it out again, and it seems that now the power supply cap is completely shot as now its humming in all 3 different power settings not just the alarm/radio mode. So it seems I will definitely have to replace the power supply caps in this radio, as well as the paper caps in there. Last edited by vortalexfan; 09-21-2018 at 07:15 PM. |
|
|