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Old 10-15-2016, 12:40 PM
Crist Rigott Crist Rigott is offline
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Join Date: Oct 2015
Location: Waxahachie, TX
Posts: 1,519
Well I changed out both resistors (R85 and R86) that were in the connector base of the 1B3GT and used heat shrink everywhere to assure no problems.

I then powered it up with the door knob cap (67) out of the circuit and I still have about 3Kv. I then reassembled the connector and cap and the same thing, 3KV.

I substituted the 1B3GT and still the same thing. I substituted the 6W4GT damper and still the same thing.

Right now I'm at a loss as to what could be the problem

I am thinking of removing the white/red wire that feeds to #1 on the yoke assembly to isolate the yoke assembly. Can I do that without causing other problems?




Last edited by Crist Rigott; 10-15-2016 at 12:47 PM. Reason: add pictures
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